So the week before Christmas, the stock clutch in my 180Q started slipping out of the blue (106K miles). I didn't want to put a stock setup back in it and was in a time crunch for the holidays as far as ordering something. I'm of the opinion that if you have the means, it's easier to remove the engine and trans rather than just the engine in our cars. This led to a full 225 conversion with donor parts from my 01. It's all OEM from TIP to tailpipe except for a custom pipe I had to fab up for the MAP since that plastic molded piece was broken on my 225, and the addition of a small port SEM intake manifold so I could use the dual SMIC setup (I sold the 225 intake mani long ago). I'm still using the AWP/180 MAF housing in the 225 TIP, and installed my adjustable FPR in the 225 fuel rail set at ~4 bar. I also swapped the 5 speed 02M out for the 6 speed 02M, along with the billet aluminum flywheel (don't know the weight) and 6 puck sprung Clutchnet disc and pressure plate from my GTI in place of the OEM setup. I also installed an 82* thermostat to help out in the cooling department and deleted the front swaybar since mine had a habit of creeping to one side ever since I replaced the cracked OEM bushing sleeve and went to poly bushings.
The screen on my phone died yesterday, so no Torque logs and I haven't broken out the VAG COM yet, but it's MUCH more responsive (lightweight FW and intake manifold) and holds boost much better into higher rpms. The DP/exhaust is giving some vibration in low rpm acceleration or high rpm engine braking, but I'm not sure where it's hitting so I need to get under the car and have a look. The trans grinds going into 5th gear only, so I need to align the linkage (didn't do that during the swap, everything felt good going through the gears with the car off) and bleed the clutch again to see if that helps. Otherwise, I'm very happy with the whole transformation that put some much needed pep in my daily driver. Since I'm still running K03 injectors and chipped software, the one 4th gear pull I did today on the way to work felt great spiking to 21 and holding ~16 psi at 6200 rpms when it limped out. I don't know if it was a boost cut or throttle closing but it was harsh, so I have some logging/tuning/tweaking to do. Logs to follow maybe this weekend.
The screen on my phone died yesterday, so no Torque logs and I haven't broken out the VAG COM yet, but it's MUCH more responsive (lightweight FW and intake manifold) and holds boost much better into higher rpms. The DP/exhaust is giving some vibration in low rpm acceleration or high rpm engine braking, but I'm not sure where it's hitting so I need to get under the car and have a look. The trans grinds going into 5th gear only, so I need to align the linkage (didn't do that during the swap, everything felt good going through the gears with the car off) and bleed the clutch again to see if that helps. Otherwise, I'm very happy with the whole transformation that put some much needed pep in my daily driver. Since I'm still running K03 injectors and chipped software, the one 4th gear pull I did today on the way to work felt great spiking to 21 and holding ~16 psi at 6200 rpms when it limped out. I don't know if it was a boost cut or throttle closing but it was harsh, so I have some logging/tuning/tweaking to do. Logs to follow maybe this weekend.